Joined
·
279 Posts
The Bachmann Annie, affectionately referred to as The R.E.K. RR Annie, came down sick this past Sunday while pulling a 39 car Coal Train at a local Hobby Show. The little engine had just proved it could pull all those cars when suddenly, it started acting very strange and was running full power even tho the throttle was set at 24 SMPH ( scale mile per hour ).
The timed chuffing and smoke were out of sync and it seemed as tho the little engine had lost it's "mind".
Not having the tools available to properly inspect the Annie and try to fix it, the owner, Stumpycc ( Cliff Couch ) decided to take the little engine home and let it rest. After consulting Annie's Doctor, Dr. DCS ( Ray Manley ) Stumpy decided to trouble shoot the problem, even tho he was fearing the worst, ( a bad DCS Board ), and the Doctor being out of town and unable to make a house call, he proceeded to open the little engine up and take a look inside.
Once the Annie was open, he discovered a partially bare wire for the motor where it plugs into the control board. But it didn't seem to be causing the problem. So, with jumper cables hooked up to the Tender and the engine plugged in, Stumpy started playing with and jiggling the wires. What he discovered was that when the wires to the brass strips along the bottom of the engine were moved, or if he squeezed the frame rails together, the motor would speed up. Also, when trying to remove excess grease from the drive train, the motor sped up and stayed there, running wide open.
After consulting Dr. DCS over the phone and thru e-mails, Stumpy decided to spray some Electro-Motive cleaner into the motor vents and around the back of the motor where the excess grease was.
I am very HAPPY to REPORT that the Little Bachmann Annie will
Live!!!!!!!!!!!!!!!!!!!!!!
I had the Doctor switch the wires on the motor connector the night before so the Annie would always start in the forward direction. ( this was a minor problem but an easy fix and one we didn't notice when we put the DCS system in the Annie /Providers/HtmlEditorProviders/Fck/FCKeditor/editor/images/smiley/msn/confused_smile.gif&160
" align="absMiddle" border="0" src="/DesktopModules/NTForums/themes/mls/emoticons/wink.gif" />
The grease from the worm gear worked it's way into the electric motor creating an internal power bleed, therefore causing the motor to go "Full throttle ".
I ran her for about 45 minutes at 16 SMPH and it didn't mess up once. I used the PFA/Direction sequence, the labored chuff, increased the throttle to 60, and then back down to normal, about 15, and it ran FLAWLESSLY!!!!!!!!!!
Cliff
The timed chuffing and smoke were out of sync and it seemed as tho the little engine had lost it's "mind".
Not having the tools available to properly inspect the Annie and try to fix it, the owner, Stumpycc ( Cliff Couch ) decided to take the little engine home and let it rest. After consulting Annie's Doctor, Dr. DCS ( Ray Manley ) Stumpy decided to trouble shoot the problem, even tho he was fearing the worst, ( a bad DCS Board ), and the Doctor being out of town and unable to make a house call, he proceeded to open the little engine up and take a look inside.
Once the Annie was open, he discovered a partially bare wire for the motor where it plugs into the control board. But it didn't seem to be causing the problem. So, with jumper cables hooked up to the Tender and the engine plugged in, Stumpy started playing with and jiggling the wires. What he discovered was that when the wires to the brass strips along the bottom of the engine were moved, or if he squeezed the frame rails together, the motor would speed up. Also, when trying to remove excess grease from the drive train, the motor sped up and stayed there, running wide open.
After consulting Dr. DCS over the phone and thru e-mails, Stumpy decided to spray some Electro-Motive cleaner into the motor vents and around the back of the motor where the excess grease was.
I am very HAPPY to REPORT that the Little Bachmann Annie will
Live!!!!!!!!!!!!!!!!!!!!!!
I had the Doctor switch the wires on the motor connector the night before so the Annie would always start in the forward direction. ( this was a minor problem but an easy fix and one we didn't notice when we put the DCS system in the Annie /Providers/HtmlEditorProviders/Fck/FCKeditor/editor/images/smiley/msn/confused_smile.gif&160
The grease from the worm gear worked it's way into the electric motor creating an internal power bleed, therefore causing the motor to go "Full throttle ".
I ran her for about 45 minutes at 16 SMPH and it didn't mess up once. I used the PFA/Direction sequence, the labored chuff, increased the throttle to 60, and then back down to normal, about 15, and it ran FLAWLESSLY!!!!!!!!!!
Cliff